Forged Engine Install
Remove and Install
Removal
Out with the old, in with the new. The motor I had in this car prior to the forged engine build blew a ring land off piston 2 years earlier. As something to get me by I swapped in a used piston from my engine build motor, It ran well but I did not trust it.
With the forged build sitting on the engine stand for over a year, I decided its time to get this project underway and finished.
First was getting the old motor out. Ive done this dozens of times before, but this time I was much carless becuase im doing this during weekdays, after a 8-10hr work day. It was more about getting this done, not getting it done cleanly.
As result, lots of fluids ended up on the floor and so floor dry was utilized a lot.
Install
The Forged Motor in all its glory. Mounting the transmission is much easier when the engine is out of the car. Before putting the transmission on however I brought it to work first, pressure washed it then painted it with a Silver Nason fast dry.
The headers were wrapped with black exhuast wrap and stainless ties. I deciede to just get a new alternator, everything else is new, why not. All the coolant hoses were replaced with Gates green strip hoses. As with other things I figured why not put a new clutch slave on, dip stick handle and crank sensor.
The engine installed, motor mounts were sand blasted and painted in Imron Elite Volcano Red.
Completed
This time around I decided that I have to much money wrapped up into this thing not to have A/C, So added it back.. new condenser, compressor, and used A/C lines. Puttin the condenser back on the car was a challenge and required some 3D printed brackets. The A/C lines also needed to be tweaked to allow the A/C Dryer to clear the Intercooler. I 3d Printed a “butt” for the Dryer to rest on the Intercooler, preventing any wear.
Well sorta completed, it turns out I had an oil leak that took quite some time to pin point, but I found it seaping out the oil pan where it it creates a half moon shape between block and transmission. It seems the RTV didnt seal completely. This resulted in dropping the oil pan, witch requires removing the rear cross member and turbo hot pipes.
It was at this time of removing the rear cross member I decided it was to difficult to remove and install, and designed an easier version. Also, this may be the only Mx6 with subframe connectors that aid in jacking up the car. I believe I made 3 sets of these, but Ive never seen them again.
Finally finished, to finish this setup off I painted the Charge pipe with Imron Elite in wrinkle gray and remade the turbo inlet with a V-Band flange and painted that in the same color.
After the first Test Drive, It runs smooth and feels like brand new car.